198U
RCHIEF
Sponsored
by-American Institute of Aeronautics and Astronautics (AIAA)
American Society of Mechanical Engineers
(ASME)
Society of Automotive Engineers (SAE)
AIAA Paper
No. 74-402
ACTIVE FLUTTER SUPPRESSION
- A FLIGHT
TEST DEMONSTRATION
by
KENNETH L. ROGER and GAROLD E. HODGES
The Boeing Company
Wichita, Kansas
and
LARRY FELT
Mr Force Flight Dynamics Laboratory
Wright Patterson Air Force Base, Ohio
AIAA/ASME/SAE 15th
Structures, Structural
Dynamics
au Materials
Contereoce
lab
V1Scheepsbouwkin
Technische Hogeschool
Delit
LAS VEGAS, NEVADA / APRL 17-19, 1974
First publication rights reserved by American Institute of Aeronautics and Astronautics.
1290 Avenue of the Americas, New York, N. Y. 10019. Abstracts may be published without
permission f credit is given to author and toAIAA. (Price: AIAA Member S1.50. Nonmember $2.00).Note: This paper available at AIAA New York office for six
months;thereafter, photoprint copies are available at photocopy prices from
ACTIVE FLUTTER SUPPRESSION - A FLIGHT TEST DEMONSTRATION t
Kenneth L. Roger. ** Larry Felt, and *Garold E. Hodges
Abstract
The first flight test demonstration of active flutter
suppression has been successfulfy completed. The Control
Configured Vehicles(CCV) B-52 test airplane was twice flown 10 knots faster than its flutter speed relying solely on an automatic
contro! system for adequate damping. The design, safety
considerations, mechanization, ground testing and flight testing
of the flutter mode control system are reported. Comparisons between flight test and theoretical results are presented. The
system was tested at heavy and light airplane weights and tested for compatibility with simultaneous ride control, maneuver load control, fatigue reduction and augmented stability.
Introduction
Modern, high performance aircraft are designed for maximum
aerodynamic efficiency with minimum structural weight. The
resulting airframe
flexibility
often leads to aeroelasticinstabilities, such as flutter. Currently, passive methods are used
to solve the flutter problem, e.g., additional stiffness, mass
balancing or speed restrictions. These passive methods result in significant performance penalties.
During the past several years, many programs have
investigated active methods of altering or controlling airframe
flexibility with flight controls. Flight tests of the B-52 and XB-70 aircraft more than seven years ago successfully demonstrated the
concept of using flight controls to
alter aircraft structural dynamic characteristics. More recently, several active control concepts have been analytically applied to a wide variety ofaircraft, including the SST, C-5A, 747, B-1, F-4, YF-16, and the Advanced Technology Transport. Some of these programs have included active control aeroelastic wind tunnel models to verify design predictions and to supplement analyses. This expanding
experience and technology base in flight control and in flutter
prediction techniques has led to the application of active control
methods to solve flutter problems with smaller performance
penalties.Reference 1 discusses the evolution of CCV technology from an idea to a B-52 flight demonstration and eventually to
the design of a prototype fighter airplane,the YF-16.
The Wichita Division of The Boeing Company, under the sponsorship of the Air Force Flight Dynamics Laboratory, is
conducting a B-52 Control Configured Vehicles (CCV) program
to demonstrate the benefits o applying advanced flight
con-trol *ecMnoioqy to a large flexible airplane. This program was
initiated in July 1971 and will be complete in June of 1974.
One of the CCV systems demonstrated during this program Nas the Flutter Mode control (FMC). FMC system uses active
aileron and flaporon control surfaces to stabilize a 2.4 Hz
ymmetric wing flutter
problem. Reference 2 discusses the;ynthesis, analysis and implementation studies of the FMC
;ystem.
On 2 August 1973 aviation history was made in the skies over western Kansas when the CCV B-52 test aircraft was flown 10
mots faster than its flutter speed. This was the first time ari
aircraft had been flight tested above its flutter speed relying
solely on an active flutter control system to augment the
structural damping. The flight was a significant step in theacceptance and incorporation of this new technology into future aircraft designs. This paper will report the details of this series of flight test demonstrations and summarize the system design.
B-52 CCV Program
Four new CCV systems were designed for flight
demonstration on the Air Force flight research airplane, NB 52E. AF56-632, which was previously used during the LAMS program. This aircraft is highly instrumented for inflight testing.
The four CCV concepts developed under this program
were Ride Control (RC),
Flutter Mode Control
(FMC).Maneuver Load Control (MLC) and Augmented Stability (ASI. The LAMS system was modified to be compatible with the other CCV systems and is denoted as the Fatigue Reduction (FRI
system. All systems were implemented using off-the-shelf
hardware and, except foP FMC, general purpose analog computets
The systems were designed to meet performance objecbvs
with each system operating individually and with all CCV
concepts operating simultaneously.
The primary goal of the Flutter Mode Control system was to
analytically extend the flutter placard speed 30 percent and
flight demonstrate the system 10 knots above the flutter speed. Compatibility with other systems was to be demonstrated up to within a few knots of the unaugmented flutter speed.
The Ride Control system tested during Phase I of the
program demonstrated a 30 percent reduction in vertical
acceleration response and a 44 percent reduction in lateral
acceleration response to turbulence at the crew station. The*
reduction met the established program goal of 30 percent reduction. The Ride Control system synthesis, design ana
analysis is presented in Reference 3 and flight test results n
Reference 4.
The Maneuver Load Control system was designed to produce
a 10 percent reduction in design wing root bending moment n the flight condition that produces maximum wing root maneum
load.
The Augmented Stability system was designed to prow required stability and flying qualities for an aircraft configuranon not meeting inherent stability requirements for Dutch roll ar short period pitch.
The Fatigue Reduction System was designed to red fatigue damage rates due to turbulence at critical wing and
fuselage locations.
Operational and performance compatibility among ìi
systems was demonstrated during Phase Il of the program.
tThis work was sponsored by the Air Force Flight Dynamics Laboratory under ContractF33615-71-C-1926. *Senior Specialist Structural Dynamics, The Boeing Company, Wichita, Kansas, MemberAIAA
**Aerospace Engineer, Air Force Flight Dynamics Laboratory, Wright Patterson AFB, Ohio, Member AIAA **Senior Specialist Control Dynamics, The Boeing Company, Wichita, Kansas, Member AIAA
pIa P41 ot arè
t t,
veus'
ex a ir Th tue in in w&g lm)càlcapi
nredìwing,'
t_n . -asid 01g p, Th wing Ittut í
Dr ¡f tIutWrAnalytical studies were conducted to determine surface
placement and size for each CCV concept and to evaluate the
potential of various configurations to meet performance
objectives. Existing B-52 control surfaces used for CCV functions
are elevators and rudder. Now additional surfaces consist of
three-segment flaperons, outboard ailerons, horizontal and a
vertical canard. Figure 1 shows the surface arrangement and
usage for each concept. The three segment flaperonreplaced the existing inboard flaps.
FMC System Design
Configuration Selection
A flutter mode within the speed capabilities of the B-52
test
airplane was created by adverseballasting of the wing drop tanks.
The left and right tanks, whichnormally carry 19,500 pounds of fuel each, were modified to carry, instead, 2000 pounds of lead
in the forward end of each tank. The lead weights were enclosed in steel and attached as shown in Figure 1. Because of the light weight of the ballast, comparedwith the normal fuel load, only
local
modifications to the drop tanks
were required. The
capability to jettison the droptanks was retained.
Figure 1. B-52 CCV Control Surfaces
At the 21,000-foot test altitude, the ballasted airplane
was
predicted to flutter at 315 knots (calibrated airspeed) with a full wing, and at 330 knots witha half-full wing both speeds well
under the normal level flight
limit of 400 knots. The flutter
mode n each case was predicted to he symmetric, about 2.4 Hz,
and mild. The rate of loss of damping was expected to be about01g per 10 knots.
The flutter mode consisted of wing 2nd vertical bending, wing ist torsion, wing ist fore and aft bending, outboard
engine
strut side bending and body nose and tail vertical bending.
Flutter does not occur if the drop tanks are either full or empty,
or if the outboard wing fuel tank is empty. Analytically the
flutter
is most severe when the ballast is 2,000 pounds (as
chosen) and as far ahead ofand below the wing as possible.
The characteristics of the flutter mode were important in
planning the entire CCVprogram:
Its mildness made testing iO knots above flutter with
a
dual FMC system feasible.
Its low frequency permitted the use of a linear, yet relatively low cost control system.
Its existence within the bandpass of the Ride Control and
Fatigue Reduction systems provided
a test
of the
adequacy of their design criteria.
2
Design Methods
One of the purposes of the program was to see whether
existing analytical methods were adequate for predicting the
performance of the new control systems. The analytical tools were conventional, except perhaps in
the scope of
theirapplication.
The structural generalized coordinates were selected by
vibration analysis, retaining the 27 lowest frequency symmetric modes (see Table i for those under 5 Hz) and, when applicable, the 27 lowest frequency antisymmetricmodes
Table I. Low Frequency Symmetric Vibration Modes Unsteady aerodynamic forces acting on the airplane were represented by the doublet lattice method, with the airplane
paneled as shown in Figure 2. .The wing, engines, body nose, tail, and control surfaces were aerodynamically coupled with each other.
Figure 2. Doublet Lattice Aerodynamic
Paneling
The interfacing of the point frequency unsteady aerodynamic
coefficients with Laplace transform equations of motion
was
done with the use of
approximating functions. Figure3 shows a
typical aerodynamic coefficient
plotted as it moves up the
imaginary axis, and the "best fit" approximating function. The approximating function chosen was a rational polynomial with
denominator roots on the left real axis. It can be considered to
be a physically realizable
frequency interpolating function for
the unsteady aerodynamic coefficients. A functionwas found for each element in the
aerodynamic influence matrix. The resulting functions were generalized and included as part of theequations of motion, raising the order of the differential equationsonce for each denominator root. Two roots (4th order equation)
were
usually used, with four roots (6th order equations) foraccuracy
checks and one root (3rd
order equations) for thehybrid
MODE (260,000 LBS)FREQUENCY FREQUENCY
(375,000 LBS) WING .88Hz .78Hz WING 1.74 1.68 INBOARD ENGINE 2.01 2.00 OUTBOARD ENGINE 2.15 2.13 WINGANDBODY WING 2.41 2.22
INBOARD ENGINES AND
BODY 2.97
2.78
INBOARD ENGINES AND
BODY 3.14
3.11
WING AND OUTBOARD
ENGINES 3.77
3.46
SURFACES RUS FMCCcv COSCE RSMLC AS FR BURDEN ELEVATOR FLAFEROS OUTBOARD AILERON HORIZONTAL CANARD VERTICAL CANARD XX I SEGMENT X X X X X X X X
ter. Because of the continuous nature of the
:imating functions the equation of motion were expected
valid in the region of theS-plane near the imaginary axis
ositive and negative damping) throughout the frequency
nalyzed.
\ DOUBLET LATTICE
CALCULATION POINTSAPPROXIMATING FUNCTiON IMAGINARY INCREASING
FREQUENCY
REAL
ure 3. Aerodynamic Coefficient Approximating Function
:hesis Constraints
Synthesis constraints were imposed on the system to assure adequate performance would be provided with variations
i that predicted by the nominal mathematical model. These traiiits provided a tolerance for variations in surface
otiveness, airplane modeling accuracy and system hardware.
i of the following constraints was evaluated independently
all other parameters held at nominal values:
.
The system will remain stable with feedback sensorlocation variations ± 60 inches parallel to the local elastic
axis.
s Stability margins will be greater than ± 6 db gain margin
at nominal phase and greater than i 60 degrees phase margin at nominal gain at frequencies below 3 Hz. The Phase margin will increase linearly to i 180 degrees at nominal gain for structural modesabove 5 Hz.
s The FMC system will remain stable in atmospheric
turbulence of the same intensity used for structural
design.
s Implementation will provide a single-fail operate
capability.
e Sustained residual acceleration osciltations in still air at
the pilot's station will be no greater than 0.014 g
peak-to-peak. (This acceleration amplitude is less than the human perceptible level.)
em Synthesis
Root locus linear analysis techniques using equations of
ion with from 18 to 27
structural modes were used to:hesize the FMC system. The large setof high-order equations
otion dictated that the studies be conducted with as many as roots. The required eigenvaluesolutions were done using the
real matrix algorithm and 16 digit numerical accuracy. A
rid computer simulation including only six structural modes
,ided the analytical method for evaluating the system
3
nonlinear effects. FMC system nonlinearities evaluated included
backlash in the actuator attachments, servovalve threshold,
control surface displacement limits and surface rate saturation. Power spectral density analyses were conducted to assess the
effect of the FMC on gust loads at critical structural locations
and to determine surfacedisplacement and rate requirements. A fixed-base piloted simulation was used to evaluate the flying
qualities.
The FMC is composed of two independent control loops,
sensors to surfaces; the outboard aileron loop and theoutboard
flaperon. Each loop sufficientlyaugments the damping to meet
system performances objectives.
To provide active
fluttersuppression, a control surface should be selected that will
generate force and moments properly phased with the flutter mode. An important consideration in wing surface location sthe relative phasing between incremental wing lift and (ocal vertical
displacement. Various combinations of sensor types and
placement were evaluated at critical flight conditions using root locus techniques to determine the phasing of the flutter mode. damping improvement and coupling with other structural modes.
The selected configuration was then evaluated at all flight
conditions.
The FMC system senses vertical acceleration at WBL 925 which is passed through a shaping filter and used to drive the
outboard ailerons. A second sensor measures vertical acceleration
at WBL 565. This signal isshaped and used to drive the outboard flaperon. One of several variations considered during the FMC synthesis was to use longitudinal wing acceleration to decouple
the flutter mode and the sixth structural mode. This signal was
eliminated later in the design process because of its
incompatibility with other structural modes at the heavy gross weight condition. Figure 4 depicts the FMC sensor and surface
locations used for the B-52 airplane. A functional block diagram of
the FMC system and associated actuatoris illustrated in Figure 5.
Z I g HIRt. 565j VERTiCAL ACCELERATIIR Z g 1.45 VERTICAL ACCELEROMETER (4 PLACES) OUTBOARD FLAPERON (NEW)
OUTBOARD AILEHONS (NEW)
Figure 4. FMC Control Surface and Sensor Locations
VOLT z-H S > .
ti'
200 ACTUATOR SECFigure 5. FMC Functional BlockDiagram
eRr? rrRucT1 MO DAME R FMC lud cri oper at i wing nd
FI4it
SYnthess tst,k f oo A 4r.eOfl .14f f eren tornI
spec wels othe Figu incu Gain ± 12' CRTA STR UC ii MODE i. S VOLT 0ES S 2.S8l ACTUATOR S HA P124 G S HA 5 124 12 VERTICAl ACCELERATILS FILTER WRL 925The FÍC system was predicted to increase flutter placard
speed more than 30 percent as illustrated in Figure 6, for the mid
weight wing (260,000 lb. gross weight). The effectof FMC on other significant structural modes (q2 and q6) are also shown.
Figure 7 shows that the FMC exceeds the goal of 30 percent
increase in Vp with the model tolerances previously discussed. Gain margin is greater than ± 14 db and thephase margin exceeds ± 120 degrees for each control surface.
.12-CRITICAL STRUCTURAL MODE DAMPING RATIO .08-' .04-0 q6 'EtEUIREMENT l3PV 380 340 380'-..-.._...40 AIrOSPEED-KCAS
Figure 6. FMC Predicted Flutter Speed Improvement
NOMINAL FMC MODE 5 TOLERANCE BAND MODE 2 TOLERANCE RAND MtNIM(JM DAMPING QUIREMENT 3vp 300 340 380 420 AIRSPEED '- KCAS
Figure 7. Tolerance Effect on Flutter
FMC compatibility was evaluated with other CCV systems
and critical airplane parameters. The 30 percent Improvement in
flutter placard speed was achieved with all CCV systems
operating simultaneously. The increase ingust loads at all critical
wing and body locations was less than threepercent.
Flight Safety Considerations
Flight safety was includedas an integral part of the FMC
synthesis and implementation. Independent sensor, electronics,
control surfaces and secondary power was used for each
feed-back loop to provide redundancy.
A safety monitor detects differences in the two outboard
aileron channels and will
shut off this system if
channel
differences exceed five degrees. The flaperon safety monitor performs the same function in a similar manner for the flaperon
system. The disengage levels of the monitors were selected to be
4
as large as possible without causing acceleration and moments to approach design limits.
Another safety feature was to hardwire the FMC system to
increase reliability (Each of the other CCVsystems was wired
on the on-board analog computers).
Since the flutter mode is a mild and only 2.4 Hz, the pilot
has adequate time to reduce airspeed before structural failure should a total loss of the FMC function occur. Piloted simulator results show that approximately five seconds are required for the pilot to react and decelerate the airplane 15 knots from speeds
above the flutter speed, using airbrakes
and throttle. The
five-second deceleration interval is much less than the time
necessary for the flutter mode to diverge to structural failure.
Figure 8 illustrates the time to reach wing design load factor
following total FMC disengage during a strong flutter test input.
7 WING TIP 5 ACCELERATION g8 4 DESIGN LIMIT AT CONSTANT -15 KNOTS ABOVE 8 FLUTTER SPEED TYPICAL 15 KNOT DECELERATION TIME
Figure 8. Wing Tip Acceleration After Total
FMC Disengage
Telemetry of selected channel of data provided real-time monitoring of the structural activity at selected locations on the test vehicle. Parameters monitored by telemetry included control surface deflections and double integrated
acceleration response at
the left wing tip
(vertical and longitudinal), right wing tip(vertical), body nose (vertical), aft body (lateral), horizontal tail
tip (vertical), and fin tip (lateral).Flutter testing was conducted using pilot inputs sequentially to the elevator, rudder, and
inboard ailerons/spoilers. FMC Mechanization
The new equipment consists of hydraulic actuators, outboard
aileron surfaces, f laperon surfaces, wing mounted accelerometers,
special control panels at the pilot and flight engineer's station,
signal shaping electronics and ballastedwing tip tanks.
The aileron and flaperon control surfaces were actuated independently. Each surface had the following chord and
spanwise dimensions:
Chord Span
(in.) (in.)
Outboard Aileron 25 101.5
Outboard Flaperon 35 95
A photograph of the test airplane with the CCV control
surfaces installed is presented in Figure 9. The aileron surfaces
PEAK FOR LINEAR DECELERATI0N STARTING 15 KNOTS ABOVE FLUTTER SPEED
- FLUTTER MODE AMPLITUDE
-
FOLLOWING FLUTTER TEST INPUT('S ITIC AL S1RUCTIJRAL MODE DAMPING .32 .24 -16 08 FUEL CONFIGURATION ANALYTICAL RESULTS I /
/
- FMCS OFF FMcsoN 80 20 40 60 TIME - SECONDS q6 MINIMUM q2 DAMPINGare mass balanced and partially aerodynamically balanced. The flaperon surfaces were not mass balanced since analysis showed the surfaces to be flutter free at the test speeds, and were not aerodynamically balanced.
I-tçjure 9. Modified Test Airplane
High performance electrohydraulic actuators are used to
drive each FMC control surface. Two critical actuation
parameters are backlash and bandwidth. Since the flutter mode becomes unstable as the FMC gain is reduced, a limit cycle is
produced for signal amplitudes less than the backlash. Total
actuator backlash was designed and verified by tests to be less than 0.175 degrees. The corresponding acceleration at the pilot's station is less than 0014 g peak-to-peak, which is less than the perceptible level. No limit cycle acceleration was perceptible during flight above the flutter speed. The bandwidth of the
actuator is approximately 6.5 Hz which provides predictable gain and phase at the 2.4 Hz flutter mode frequency.
Control of each CCV system is accomplished through panels located at the pilot's and flight engineer's stations. A picture of
the pilot's engage panel is presented in Figure 10. The flight
engineer's panel is similar. To engage a system the flight engineer
determines that the mode is
functional and depresses theassociated system switch. When the pilot depresses his
corresponding mode switch the system becomes operative. Only the pilot can engage a system, but both he and the flight engineer
can disc'nn' crstem.
Figure 10. Pilots Engage Panel
System Ground Tests
Prior to beginning the series of flight tests, an extensive ground test of the FMC implementation was accomplished to assure airplane and system flightworthiness. A block diagram
showing the mechanization of these ground tests is presented in
Figure 11. Special test inputs are introduced from (1) the
5
on-board signa? generator to determine hysteresis and slfp
response, (2) the transfer function analyzer to determoi frequency response, and (3) the flight engineer's test panel 1 confirm correct system operation during preflight checks. lev
inputs may also be introduced from the FBW pilot's cont'o.
Responses to test inputs are recorded on an X-Y plotter, or x
on-board oscillograph, from on-board digital voltmeter readii or the transfer function ana?yzer. A matrix is presented in Fisse 12 that shows the different types of component and system ie
conducted.
r=
G C -10 .20 -loo N .0 G -200 -300 01/
H
w' H
DESIGN GA 'I'OLERANCE A_VObO uniS_S_uns 1.0 FREQUENCY . liz IO rocarr e ,IOrat .*.fl Á-innig fins nrtM nfl OeRO&J flY000tUCPOWti iNflictS DtfllflflHIi
Figure 11. Ground Test Mechanization
Figure 12. System Ground Test Matrix
The L.H. outboard aileron actuator frequency reponse I'tI'W
in Figure 13 is typical of ground test results for ballt ø4
actuators. All actuators were implemented with a pisto orifice to provide damping and a notch filter in the forrd 1i:
of the actuator loop to achieve the required closed loop 'eul The orifice was sized to provide a minimum damping (g o The notch filter does not augment damping but deco
'eo!
actuator-surface mode from airframe structurai ma
reducing the response amplitude. As shown, both o tf methods of compensation are required to meet the att.
tolerances.
t.'
t, i DESIGN PHASE TOLEUANCEFigure 13. Outboard Aileron Ground Test Frequency WIidz
AGItATORS 019W CONIROl. fl CLtVTY PILOT SMC SENStS1S H O .1 Z H E ACCOLER. OMETESIS O , 0LIT. flO1 WT FREQUENCY RS:oroNslO X IC X X X X X O CALSATSON, SCALEbANDPHASINC XX XXX X X X
XXX
X }ÍVSYFO.ESR X X X X X X X X X X O STEP RESPONSE X X *r"' LJ-
,-
niwaan
'
'-ET' fi EQ CN NCY S-Y PNSDTYR pun REONU l'uEruC,rr TES_VS SEER)R TOPAIt flOTTAI vOLuME_Vii- - - WITH NOTCH FILTER-WITHOUT NOTCH FILTER
The measured actuator surface resonance was 23.5 Hz compared to a predicted frequency of 31 Hz. The predicted resonant amplitude was +6 db compared to the measured amplitude of +7.5 db. The flaperons were tested in a similar
manner and showed similar agreement with analytical
predictions.
Prior to each flight the FMC system was functionally tested
as a part of the routine preflight tests using end-to-end step
responses.
Flutter Test Results
During flutter testing, the existence of the baseline (systems
off) airplane flutter mode was verified. The flutter speeds for
both the 260,000 pound and 375,000 pound configuration were about seven percent higher than predicted, as shown in Figure
14.
.06
DAMPING-. g
.04
Figure 14. Test and Predicted V-g, FMC Off
The FMC performance was satisfactory and the test objective
of flying 10 knots past flutter was met or exceeded for both
gross weights. The speed-damping (V-g) plots for these flights are shown in Figures iSa & 15b. The airplane remained above the
FMC-off flutter speed approximately four minutes for each configuration, while the pilot performed normal flutter testing.
.02
o O 240 300VELOCITY KCAS
21,000 FEET
- THEORETICAL
O TEST 375, 000 LBS.00
240 300VELOCITY KCAS
Figure 15a. Test V-g, FMC On
400
DAMPING g
.04
.06
.02. o 240 300VELOCITY KCAS
Figure 15b. Test V-g, FMC OnAddition of the Maneuver Load Control, Ride Control, and
Fatigue Reduction Systems further increased the damping of the
lowest damped wing mode as shown in Figure 16. No CCV system or combination of systems caused a reduction of the
flutter speed below that of the basic airplane.
21,000 FEET
375,000 LBS.
o FMC
Q BASIC AIRPLANE
40021,000 FEET
260, 000 LBS.D
FR + MLC + FMC + ECS O BASIC AIRPLANE Figure 16. Test V-g, FMC, MLC, RC, FRTest telemetered and predicted transient responses 10 knots
below flutter for a typical pilot flutter test elevator input are
shown in Figure 17. The predicted response was obtained by inverse Laplace transform using a 24 mode set of equations of
motion, and includes the telemetry ground station double
integration and
filtering. The slow beating of the wing tip
response which might otherwise have been alarming during test, was predicted accurately.
400 240 300
VELOCITY KCAS
.1021,000 FEET
260, 000 LBS. O FMC.08
0
BASIC AIRPLANE 10.08
WING TIP LONGITUDINAL
COCKPIT VERTICAL
WING TIP VERTICAL
WING TIP LONGITUDINAL
àAIàA&a
.
COCKPIT VERTICAL
r260,
000 LBS. 21, 000 FEETWING TIP VERTICAL
1/Nf
WING TIP VERTICAL
E-.
r
WING TIP LONGITUDINAL
E-Ii
i I f I I I IIi
0
1 23 4567 8910111213
TIME - SECONDS
Figure 18. Test Transient Response, 2 Knots Below Flutter,
With and Without FMC
The transient responses of the FMC control surfaces, the
pilot test input, and the cockpit vertical acceleration are shown n Figure 19, flying 12 knots above the (FMC-off) flutter speed
with FMC engaged. The pilot input was sufficiently strong to
cause vertical accelerations at the cockpit in excess of 1g
incremental. The flaperon required a peak deflection of only four degrees and the outboard aileron only three degrees.
Figure 17. Test and Predicted Transient Response, 10 Knots
Below Flutter
Test transient responses two knots below FMC-off flutter are shown in Figure 18, both with and without FMC. Without FMC, the flutter mode was essentially neutrally stable.
21,000 FEET 375,000 LBS.
WING TIP VERTICAL
WING TIP LONGITUDINAL
7 DEGREES 1.0 .8 .6 .4 .2 g's .0
-.2
o 6 4 2 o -2 -4 -6 6 4 2 DEGREES o -2 -4 -6 10-4 DEGREES -6-21.000 FEET 3'75,000L.
COCKPIT VERTICAL ACCELERATION OUTBOARD AILERON (FMC)
FLAPERON (FMC)
ELEVATOR (PILOT)
0 1 2 3
TIME - SECONDS
Figure 19. FMC Transient Response, 12 Knots Above Flutle6
The pilots reported the FMC system made the airplw
response typical of the most stable B-52 configurations.
The flight demonstration of active flutter suppression ws
completed successfully. The analytical methods used to piethct
the flutter, the controllability of flutter, and the hdwxe
performance wore, when used with the specified design criter and tolerances, adequate for the task. The hardware perform
was predictable analytically to frequencies much higher thr
required for this test.
The authors' opinion was strengthened, on the basis of tIvT
tests, that whenever structural and aerodynamic theo
irr
adequate to predict flutter, the controllability of flutter s IlK
predictable. Whether FMC is applicable to more violent, hiw
frequency modes can then be decided analytically for ' specific airplane. For those cases where wind tunnel testina necessary to determine flutter, tunnel testing of the active PIC
system will be equally necessary - parameter dent,iicatier
methods will need to he developed to support experirnenl
control synthesis.
These flights have demonstrated that the benefits enC
penalties, mechanization and operation of active flutter corirti
systems are within the scope of current engineering antt
methods. The successful conclusion of a flight flutter te
program is to report that nothing very surprising happened
References
Johannes, R. P. and Thompson, G. O., "B-52 Corrt,i
Conf igured Vehicles Program".
Hodges, G. E., "Active Flutter Suppression - B-52Cr'c* Configured Vehicles".
Stockdale, C. R. and Poyneer, R. D., AFFDL-TR 7343 "Control Configured Vehicle Ride Control System
RCS) B-52 Control System Analysis, Synthesss,
Design".
4. McKenzie, J. R., "B-52 Control Configures Vehicles I*
Control Analysis and Flight Test".
T ito