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OTC 6488

Upheaval Buckling Failures of Insulated Buried Pipelines:

A Case Story

N-J.R. Nielsen and B. Lyngberg, Maersk Olie & Gas AS, and P.T. Pedersen,

Technical U. of Denmark

Copyright 1990. Offshore Technology Conference

This paper was presented at the 22nd Annual OTC in Houston. Texas, May 7-10,1990.

This paper was selected for presentation by the OTC Program Committee following review of information contained in an abstract submitted by the author(3). Contents of the paper, as ç nted, have not been reviewed by the Offshore Technology Conference and are subject to correction by the author(s). The material, as presented, doesnot necessarily retiedi any ;ion of the Offshore Technology Conference or its officers. Permission to copy is restricted to an abstract of not more than 300 words. Illustrationsmay not be copied. The abstract should contain conspicuous acknowledgment of where and by whom the paper is presented.

Laboratorium voor Scheepshydromecbanica

Archief

Makelweg 2,2628

CD Delft

Tel.: 015-7868'73 -Fax:015.781836

terfield pipelines in the Danish Sector of

the North Sea.

It is the objective of this paper to pre-sent the case story of this pipeline up-heaval giving a chronological description

of all actions taken, in order to

re-estab-lish the pipeline integrity.

Based on the upheaval buckling experience within Mmrsk Olie og Gas AS, a recommenda-tion for the design and installarecommenda-tion of buried, hot pipelines is presented.

INTRODUCTION

L_zing the annual pipeline inspection survey in July 1986 along the buried Rolf A/Gorm E two phase pipeline in the Danish

Sector of the North Sea, a pipeline section

was discovered to have protruded the sea-bottom, and was standing in an arch. The 17 km long pipeline is an O.D. 8.625" x WT 14.3 mm carbon steel line (API 5L grade X 52). The pipe is insulated with a 2" thick polyurethane foam (PUF) of min. density 96

kg/m3 encased in a high density polyethylene

(PE) jacket. The exposed PUF at the ends

of the PE jacket is sealed with water tight end cap sleeves. A 2" thick concrete weight

coating is applied on top of the PE jacket resulting in an overall pipe diameter of 0.45 m. A 3" gas lift line is "piggy bac-ked" to the 8" pipeline. The pipeline

References and illustrations at end of

paoer.

The pipeline was laid in the summer of 1985 in 40 m water depth utilizing conventional lay barge techniques. Trenching of the line was carried out using water jetting equip-ment.

The pipeline was brought into service January 1986 for transport of unstabilized

hydrocarbons with a temperature of up to

180°F (82°C) from the Rolf satellite field

to the central process facility at Gorm.

Upheaval buckling analysis of the 8" line was carried out as part of the design documentation resulting in a lowering requirement of 1.15 m to top of the con-crete coated pipe. The certified upheaval

buckling calculations were performed accor-ding to the state-of-art at that time, i.e.

using the "classical" upheaval buckling

analysis, where the design criteria against

upheaval snap buckling is based upon post

buckling equilibrium curves assuming a pipe

of uniform weight on a rigid foundation.

Following the detection of the exposure an upheaval buckling research programme was immediately initiated at the Technical

University of Denmark. The results from the

study showed that the "classical" design approach did not always yield conservative

results. Thus, a new and improved

theoreti-cal model was developed and made available late 1986, and formed the basis for the repair work. The new design approach has been published in ref. [2], [3] and [4].

581

ABSTRACT

The first recognized upheaval buckling of build-up is shown in Figure 1, and a

detai-a subsedetai-a, buried pipeline took pldetai-ace in led description of the pipeline is given 1986 in one of Mmrsk Olie og Gas AS' in- by Pallesen et.al. (1985) in ref. [1].

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DETECTION OF EXPOSED PIPE AND ACTIONS TAKEN AA-found Survey (let Upheaval).

f0F.n During the 1986 annual inspection survey along the buried 8" Rolf A /Gorm E

pipe-line, an exposed pipe section was detected from side scan sonar records at a distance of 0.3 km (KP 0.3) from the Rolf platform.

A subsequent diver inspection of the ex-posure revealed a very localized pipeline

upheaval,where the apex of the buckle

mea-sured to the bottom of the pipe protruded

1.1 m above seabed level leaving the

pipe-line free spanning over a 10 in section,

see Fig. 2. The apex of the buckle coin-cided with a field joint, and it became evident that the steel pipe at this loca-tion was subjected to a relatively severe bending curvature. An estimation of the

induced strain showed that a strain in the

order of 3.5-8.0% was likely to have oc-cured, which meant that the pipe cross

section had undergone plastic deformation.

To determine the overall buckling

confi-guration, diver probing of the burial depth

on both sides of the exposed pipe was carried out. The results of the probing showed that the buckle wave length was

confined to 24 m corresponding to two pipe joints.

As the burial depth to bottom of the

"un-disturbed" pipeline sections to either side

of the upheaval was approx. 1.5 m, the

overall buckling amplitude became of the order of 2.6 m. Fig. 3 shows the buckled pipe section after having been retrieved

from the seabottom and transported to shore. It is noticed that the resulting up-heaval configuration has similarities with

a plastic "hinge" failure.

Immediate Safety Measures

At the time, in July 1986, when the

pipeli-ne upheaval was discovered, the lipipeli-ne was

operating at a pressure of 1,000 psig

tran-sporting approx. 10,000 barrels daily of unstabilized oil with a flowing tubing head temperature (FTHT) of 176°F (80°C).

During the service period (7 months) prior to detection of the upheaval buckle the pi-peline had been subjected to 15 major shut-downs varying between 1 and 17 hours

(aver-age duration was 5 hours). Assuming that

the upheaval had occured at an early stage

in the service period, the susceptibility

to "low cycle high strain" fatigue was eva-luated to be critical, in particular in the welding area, where relatively large stress

concentrations exist.

Consequently, in order to minimize the risk

of a rupture in the plastically deformed

pipe, the following safety precautions

were taken:

582

Maintain steady production (constant

temperature and pressure) .

Monitor the upheaved pipeline configura-tion.

Dedicate a guard vessel to patrol at the upheaval location for protection against third part damage (e.g. fishing activi-ty).

Establish procedures defining remedial actions in case of observed

abnorma-lities.

The 3" piggy back line had not yet been taken into service as a gas lift line and therefore did not present a potential

safety hazard.

The relevance of precaution No. 1

(elimina-tion of low cycle fatigue) was verified upon shut-in of the line prior to the

repair work as contraction of the line upon cooling down lowered the apex of the

uphea-val section from 1.1 m to 0.55 in above seabed level, see Fig. 2,

ASSESSMENT OF DAMAGE

In order to find the technically and

econo-mically most feasible repair strategy, a detailed assessment of the damage caused

by the upheaval was undertaken. In

particu-lar the investigations were concentrated

on

Strain/ovalization Low cycle fatigue Amount of foam damage

Determination of time ot upheaval

The ratio between the outer diameter and

the wall thickness of the 8" steel pipe is

15.3. Such "compact" pipes normally have sufficient capacity to form a plastic

bending mechanism without significant

flattening.

Thus, it was concluded that the

cross section was not subjected to severe

ova lization.

The "low cycle high strain" fatigue life of the pipe at the apex of the buckle was

estimated to 20-25 cycles of 3-3.5% strain. Based on the production history (number of shutdowns), it was calculated that: the

remaining fatigue life at the time of detection was 10-15 strain cycles of 3-3.5%. The strain of 3-3.5% was estimated to correspond to one complete shut-down assuming an initial induced strain of 8%. However, as no "low cycle high strain"

fatigue data was available for the

materi-al in question, these cmateri-alculations were subjected to some uncertainty.

2 UPHEAVAL BUCKLING FAILURES OF INSULATED BURIED PIPELINES - A CASE STORY OTC 6488

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ue to the longitudinal expansion of the 8" steel pipe at the upheaval location, relative movements occurred between the PUF/PE-sleeve interface causing the foam to slide approx. 50 mm out of the sleeve and damaging the end cap sealings. This bond breakage could have taken place for a considerably distance on both sides of

the upheaval. Also, there were indications

that a shrinkage of the foam had taken place. After having retrieved the damaged

section, the severity of the foam shrinkage

became evident. The foam had collapsed to

half the original thickness, see Figure 4.

By evaluating the biological parameters of the marine growth on the exposed pipe

section, it was concluded that the upheaval

was most likely to have taken place in January 1986, i.e. within the same month

the pipeline had been brought into service.

DETAILED PIPELINE SURVEY

ollowing the detection of the pipeline

upheaval at KP 0.3, it was decided to carry out a comprehensive sub-bottom profile

(SBP) survey along the entire length of the

pipeline in order to determine the in-situ condition of the pipeline burial and

pipe-line profile.

The SBP survey started in September 1986 with pipeline crossings at approx. 10 in

intervals utilizing a remotely operated vehicle (ROV). The 10 in crossing interval

was selected as a compromise between survey

costs and required number of SBP measure-ments in order to resolve pipeline undula-tions with 20-30 m wavelength.

During the execution of the SBP survey a second pipeline exposure was found at a distance of 2.2 km (KP 2.2) from the Rolf

platform.

This exposure did not exist at the time of -he annual pipeline survey in July 1986,

_.e. the pipe had upheaved between late July and early September 1986. The sub-sequent diver inspection revealed a 5 in

pipeline exposure with a maximum height of 0.2 m above seabed level measured to the bottom of the pipe. As for the first up-heaval at KP 0.3 the imperfection wave length was confined to 24 m. The overall height of the buckle was of the order of

2 m.

No further exposures were found along the pipeline. However, at 26 locations the

pipeline was subjected to severe vertical undulations, i.e. imperfection amplitudes

of 0.5-1.0 in with a corresponding wave

length of 50-70 m. The minimum depth of

cover at these locations varied between 0.4

m and 1.4 in as compared to the generally obtained lowering depth of 1.6-1.9 in to top of pipe.

583

Thus, upon completion of the detailed SBP survey the state of the pipeline could be summarized as follows:

Upheaval buckle at KP 0.3

Upheaval buckle at KP 2.2

Excessive vertical undulations of unex-posed pipeline sections at 26 locations.

CAUSES OF OBSERVED UNSTABLE PIPELINE BE-HAVIOUR

Installation Induced Imperfections

In order to explain the causes of the

observed unstable pipeline behaviour the

history of the pipeline was closely exami-ned.

It was known and documented that the

pipe-line had been subjected to trawl gear

im-pact at about 10 locations along the pipe-line route prior to trenching of the pipe-line. The upheaved section at KP 0.3 had

experi-enced such trawl gear impact causing da-mage to the 8" line and laterally displa-cing 6 joints (72 m) of the 3" piggy back line up to 2 in from the 8" pipe, leaving

a permanent bend in the 3" line. Trawl gear "pull-over" calculations indicated that also the 8" steel pipe had been stressed beyond the elastic limit. At a further 5 locations the 3" line had been damaged

with displacements up to a maximum of 10 m from the main line.

During lowering of the pipeline all sec-tions, which had been hit by trawl boards

were temporarily left untrenched to provide

access for detailed inspection and sub-sequent repair work, if required. Upon

trenching of the repaired sections, the

resulting pipeline configuration in the transition zones becomes as shown on Fig.

5.

An analysis of the bending stresses induced

in this condition is shown in Fig. 6, as a function of the untrenched length for

different depths of burial. In the present

case, it was found that the linear cal-culation model predicted stresses which

exceeded the yield stress by typically 23%. Therefore, some plastic deformation of the pipeline was expected to have been introdu-ced during the subsequent trenching

opera-tion. Furthermore, the starting and stop-ping of the trenching at these locations

would almost certainly have introduced some

level of foundation imperfection over and above that to be found in sections where

trenching had been performed in one conti-nuous pass.

A change in the operating parameters of the

trenching equipment and variable soil

conditions along the pipeline route could further result in an irregular pipeline

profile.

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for this idealized model, where the foun-dation is assumed to be rigid. The bifur-cation load is infinitely high. As the limiting permissible temperature rise is taken the minimum temperature on the U-shaped postbuckling equilibrium curves in

the temperature-buckling wave length plane,

such as Fig. 8, or temperature-buckling amplitude plane. For perfect pipelines without initial imperfections such a pro-cedure will be conservative.

During the design phase also the effect of

imperfections was discussed. This discus-sion was related to Fig. 8, which

schema-tically shows how the response will differ

from the one predicted for the perfect

geometry case. It was concluded that since the adopted "trough" criterion is not very

sensitive to imperfections the proposed design should be conservative also for

pipelines, which invariably posses initial imperfections.

The result of these numerical calculations was that for a design temperature of 200°F

(93°C) and an internal pressure of 3,000

psig (20.7 MN/m2) the required minimum soil

cover was 0.90 in to top of the 8" pipe. The design trench depth was then taken as

1.60 in giving approx. 1.15 in soil cover to

top of the 8" line.

The trenching analysis performed for the pipeline was based on a method suggested by Mousselli [5]. The theoretical back-ground for this analysis is a beam model,

where the pipe is assumed elastically sup-ported by a concentrated soil spring at the

edge of the trench, see Fig. 9. Assuming

a relatively rigid

foundation

and an

allo-wable maximum bending stress equal to 305 MN/m2 (0.85% SMYS), it was found that the

maximum trenching depth was 1.6m, and that an increase in trench depth of 20 cm would

increase the stress level by 4%.

A New Design Procedure

In order to get a consistent theoretical basis for the repair of the pipeline, it was obvious that a new mathematical model needed to be developed.

During this analysis work it was shown that a buried and heated pipeline section with an initial imperfection can lift

itself upwards upon experiencing the

opera-ting temperature, by slightly lifopera-ting the overburden without necessarily being able to break out of the soil, i.e. without upheaval snap buckling. During a Later

shut-down the line will cool down and try to return to its original position. Now, during the period with uplift, sand

par-ticles will have tended to fill the "cavi-ty" below the pipeline created by the

uplift. Thereby, a complete recovery to the

original position is prevented. Hence, at

sections of the pipeline with initial

imperfections above a certain limit the Time Dependant Upheaval behaviour

Whereas the first upheaval at KP 0.3 was

considered a classic upheaval buckling case (upheaval snap buckling) the second

uphea-val at KP 2.2 could not be so easily ex-plained owing to its apparent time

depen-dency, i.e. the upheaval took place between

the annual inspection survey in July 1986

and the SBP survey in September 1986. Also,

from the time of detection of the first

upheaval until the decision of maintaining

steady production was taken the line was

subjected to 4 additional shut-down

situa-tions of which two were major.

By comparing the detailed SBP (1986) survey with the as-built (1985) survey documenta-tion, it became evident that certain pipe-line sections with initial vertical "imper-fections" had moved their way upwards through the soil. An example of such

obser-ved imperfection growth is presented in

Fig. 7, showing that an initial

"imper-fection" height, which in 1985 was 0.5 m, had grown to 1.0 in in 1986, reducing the

local soil cover from 1.2 m to 0.7 m. Rel-ating the 0.5 in increase in "imperfection" height to the totally 17 major shut-downs,

the average growth rate becomes 30 mm per

temperature cycle.

Following the above observations, it became clear that the classical upheaval buckling

analysis applied during the design phase was insufficient. It did not model the

detrimental effects of plastic deformation

of the pipeline in combination with lack of straightness and it could not explain

that the geometric imperfection amplitudes

were growing with time.

DEVELOPMENT OF A THEORETICAL MODEL

Analyses performed prior to installation

Prior to installation, upheaval buckling analyses had been carried out in order to

determine the necessary depth of burial and an independent analysis appraisal had been

performed by a classification society. In

both cases the analysis procedure was

iden-tical to the "classical" calculation per-formed for analysis of vertical stability of railroad tracks.

Following this approach the problem was formulated as a heavy, elastic beam on a rigid flat foundation where the weight of

the beam includes the weight of the 8" and 3" pipes and the weight of the cover soil. The solution procedure places the pipe into

a buckled configuration and seeks to find

the temperature and internal pressure which

can maintain equilibrium with a prescrited length L of the pipe in the buckled

posi-tion. This analysis produces postbuckling equilibrium curves which can be reached, if the pipe is sufficiently disturbed. A

normal bifurcation behaviour does not exist

584

4 UPHEAVAL BUCKLING FAILURES OF INSULATED BURIED PIPELINES - A CASE STORY OTC 6488

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'-perfection amplitudes will grow with the .mberof temperature changes such that the

local soil cover will decrease and at a certain stage upheaval snap buckling can

take place.

This upheaval creep mechanism resembles the

well known phenomenon seen in farm fields in the spring time where the frost drives buried stones up to the surface.

The theory behind this new design procedure

against upheaval creep is semi-analytical and easy to apply. It was implemented on a PC, and the theoretical background has

since been published in [3). It was decided

that in order to avoid that heating and cooling of the pipeline shall cause a growing foundation imperfection, a design criterion should be that, at the maximum pipeline pressure and temperature, the

maximum uplift displacement should be restricted to typically 20 mm. At KP 0.3 the foundation imperfection amplitude was timated to be 0.2-0.4 in and the wave

-_,ngth to be 24.5 m (two pipe joints). Due to the large bending moments induced in the pipeline during trenching, a plastic

defor-mation of the same form was assumed. Se-veral shapes of the imperfection were

analyzed. As an example Fig. 10 shows

relations between the minimum trench depth H and the allowable temperature differenti-al AT for three different imperfection

amplitudes, all prop-shaped. From Fig. 10, it is clear that for a maximum temperature rise equal to 80°C and the estimated

imper-fection amplitudes upheaval creep had to be expected to take place for a trench depth of 1.5 m.

This semi-analytical linearized analysis procedure [3] is rapid and easy to apply.

This is also illustrated in ref. [2], where

the procedure was subsequently used to study the design and installation of

va-rious pipelines and where requirements were 9-itab1ished for acceptable

out-of-straight-3s of these pipelines. Of course, the linearized analysis procedure can only be expected to be sufficiently accurate for

analyses connected with design against gradual upheaval caused by temperature

fluctuations, where the upheaval

displace-ments are small.

To overcome this shortcoming, a non-linear theoretical model was developed, which could be used to study the final upheaval event where the pipeline comes out of the sea bottom, see Fig. 11. This non-linear analysis procedure was also implemented on a PC. A detailed description of the mathematical background for the method has been presented in [4].

The iterative procedure uses, as start configuration, the linearized solution

produced by the upheaval creep analysis and

the mathematical model includes non-line-arities caused by:

585

Geometric non-linearities due to large deflections of the pipeline.

Non-linear stress-strain behaviour of the pipeline material.

A soil uplift resistance, which varies with the uplift displacement.

Variable or deformation-dependent axial

friction forces.

Numerical results are presented in Fig. 11

showing temperature difference AT versus

upheaval clearance A between the

founda-tion and the pipeline at the apex, for the

case of a trench depth equal to 1.5 in in "cemented" sand. The foundation imperfec-tion amplitude is 0.20 in and, as before, the pipeline is assumed to be stress free in this shape. Included in this figure is the result of the classical heavy elastic beam calculation. It is noted that the

equilibrium curve produced by the classical

procedure differs considerably from the result predicted by the more correct cal-culation procedure.

Besides the above-mentioned limitation on the allowable pre-buckling displacements, in order to avoid upheaval creep, it is also necessary to impose restrictions on how close the post-buckling equilibrium

curve should be to the points of operation

on the pre-buckling path. The latter

cri-terion is necessary in order to avoid snap-through buckling due to small disturbances.

Verification of Mathematical Model

To illustrate the correlation between predictions based upon the theoretical model and the observed upheaval creep behaviour, the "imperfect' pipe section shown in Fig. 7 will be considered. The basis is the assumption that the observed as-built out-of-straightness corresponds to the shape of a "propped" pipe section.

The free span equilibrium wave length

asso-ciated with a prop height of 0.5 in can be calculated to 46 in (airfilled pipeline).

Such an imperfection configuration has been

drawn in Fig. 7. It is seen that the shape of a "prop imperfection" shows good

agree-ment with the as-built survey measureagree-ments.

Two non-linear upheaval buckling analyses of this "prop imperfection" are presented in Fig. 12 showing pre- and post-buckling equilibrium curves in a temperature versus uplift displacement coordinate system. The difference in the response of the two curves is caused by the effect of plastic deformation of the pipe, i.e. the upper curve corresponds to a pipe without an

initial geometric pipe imperfection whereas

the lower curve includes an initial geo-metric pipe imperfection equal to the

foundation imperfection. That is, in the latter case the pipeline is assumed to be stress free in the propped configuration.

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6 UPHEAVAL BUCKLING FAILURES OF INSULATED BURIED PIPELINES - A CASE STORY OTC 6488

During the 7 months service period, the temperature difference at the "imperfect" location did not exceed 55°C. Compared to

the calculated peak (instability)

tempera-ture of 65-70°C no upheaval snap buckling should be expected, which is in agreement with observations. However, it is noticed that the crown uplift at a temperature

difference of 55°C for the pipe in the

pre-buckling stage varies between 10-40 mm dependent upon the degree of plasticity

assumed for the pipe section. With a depth

of burial at the apex of the imperfection of 1.2 m, the uplift displacement corre-sponding to peak uplift resistance in the

soil would typically be in the order of 20

mm. Consequently, for uplift movements in excess of 20 mm local shear failure could

be expected in the soil resulting in a

non-reversible flow of sand around the pipe.

Upon cooling of the line the redistributed sand particles and the non-linear pipe/soil

interaction prevents the line from

retur-ning to the original position resulting in

an upward ratcheting effect.

The conclusion is that even if it is not

possible, yet, to predict the speed of the

upheaval creep, then correlation studies such as the one presented here show that the new mathematical model is a useful tool to predict when upheaval creep is a potential problem. It also gives a good

indication of the order of magnitude of the

displacement growth for each load cycle.

REPAIR

On the basis of the damage assessment per-formed on the upheaved sections KP 0.3 and

KP 2.2, the detailed out-of-straightness

survey and the developed theoretical model the required remedial repair work was defined. The repair work included the

replacement of line pipe at the two exposed

sections and rock dumping of areas which

were susceptible to upheaval buckling

failure.

Repair at KP 0.3 and KP 2.2

It was decided to replace 6 joints of 8"

and 3" line pipe at each of the two exposed

sections by deburying the affected line

pipes, cutting out the damaged pipe joints

and replacing them by a spool piece, 6

joints (i.e. 72 m) in length using hyper-baric welding. Following the hyperhyper-baric welding of the new spool pieces rock

dum-ping was carried out to backfill the ex-cavated trenches. The rock dump was re-quired to ensure the necessary overburden on the pipeline and thus prevent upheaval

of the sections upon start-up of the

pipe-line. The repair work was carried out in October/November 1986 and each hyperbaric repair took about 3 weeks.

588

The decision to replace line pipes at the exposed areas was taken because:

The upheaved sections had been subjected to significant, but partly unknown accumulated plastic strains.

The apparent breakage of the bond

bet-ween the polyurethane foam and the

poly-ethylene sleeve at KP 0.3 reduced the longitudinal frictional resistance on either side of the upheaval increasing the pipeline's susceptibility to large upheaval movements. The upheaval at KP

2.2 would most likely have been

subjec-ted to "similar" bond breakage.

An additional important aspect of the repair at KP 0.3 was the pipeline expansion

at the Rolf riser. Because the observed bond breakage between the insulation foam and the sleeve could extend for a consi-derably distance around the region at KP 0.3 the max. allowable expansion at the riser could be exceeded. As the riser was

designed to take up the pipeline expansion

by bending of the riser pipe an excessive pipeline expansion could overstress the riser. Thus, in order to ensure a "high"

longitudinal frictional resistance for the

repair spool regardless of the condition

of the bond between the foam and sleeve the

expansion forces in the steel pipe were transferred directly to the concrete

coa-ting via "anchors" welded to the steel pipe at the spool ends. Further, all field joints in the spool were filled with con-crete instead of the original foam, in order to assure that the compressive loads were transmitted through the length of the

spool piece.

Remedial Rock Dumping

At a total of 31 locations (incl. the two repairs at KP 0.3 and KP 2.2) along the pipeline route the safety margin against upheaval buckling was found inadequate.

Therefore to re-establish the integrity of

the line in accordance with the original design condition an increase of the over-burden at these locations was necessary.

The most feasible solution was found to be

rock dumping of the affected areas. The

rock dump requirements could be related to

the following criteria:

To prevent upheaval of the newly

re-paired sections.

To prevent upheaval buckling of sections

where the foam/sleeve bond was broken.

To avoid excessive riser expansion at

the Rolf platform.

To prevent a growing "imperfection" amplitude of buried pipeline sections with significant vertical undulations.

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pon the completion of the remedial rock dump a total of 4.5 km pipeline had been

covered with a rock berm of height varying from 0.8-1.6 m. The berm plateau width was

taken as 4.0 m to account for lateral survey inaccuracy.

INSPECTION OF RETRIEVED PIPELINE SECTION

The section retrieved from KP 0.3 was taken

into the testing laboratory to test the

remaining fatigue life of the most strained

section, which had caused great concern just after the detection of the first

upheaval. The pipe was first subjected to 50 cycles of 1% strain after which the strain was increased to 3.5% and the fai-lure occurred after 6 full cycles. These tests confirmed the estimated remaining

fatigue life made at the time of the

detec-tion of the first upheaval.

Following the observed shrinkage of the nsulation foam at the first upheaval _ocation, KP 0.3, laboratory tests were carried out using foam samples from the retrieved pipe sections as well as from

spare pipe joints taken from the "emergen-cy" storage. The results of the investiga-tions showed that the foam tended to shrink

to approximately half its original thick-ness when exposed to a combination of water, temperature and hydrostatic pres-sure. None of these effects in isolation were found to cause the shrinkage.

Thus, water tight end cap sleeves are of paramount importance in order to prevent a detonation of the polyurethane foam. RECOMMENDATION FOR DESIGN AND INSTALLATION OF BURIED HOT PIPELINES

Following the Rolf upheaval buckling cident and the Mmrsk Olie og Gas AS

in-house experience from installation of "hot"

nipelines, a summary of essential aspects

1.thin upheaval buckling design of buried

pipelines is presented:

It shall be documented that buried pipelines will not be subjected to a progressive upheaval creep failure (limitation of crown uplift movement).

It shall be documented that the pipeline

has sufficient safety against a snap through buckling failure (width of

temperature-upliftdisplacementcurve). Upheaval buckling analyses shall be

based upon a consistent mathematical theory, which is capable of modelling the uplift behaviour of "imperfect"

pipelines taking into account the linear pipe/soil interaction and non-linearities of the pipe material.

587

The imperfection configurations used at the design stage should reflect typical imperfection configurations, which could

be generated during the installation (e.g. a prop type imperfection).

A scenario of critical pipe out-of-stra-ightness configurations for given burial depth shall be established (requirement

to trenching contractor).

Upon installation of the pipeline the

achieved out-of-straightness and depth-of-burial shall be measured with

suffi-cient accuracy to verify that the in-stalled pipeline fulfills the design

requirements. This will enable remedial

actions, e.g. rock dumping, to be em-ployed in case of a violation of the design requirements.

The as-built documentation shall form the basis for the subsequent annual

inspection surveys such that "critical"

pipeline sections can be monitored for possible upheaval creep (preventive

measure).

ACKNOWLEDGEMENT

The authors wish to thank the management of Marsk Olie og Gas AS for their

permis-sion to publish this paper.

REFERENCES

(1] Pallesen, T.R., Braestrup M.W., Jor-gensen 0. and Andersen J.B.:

"Insulated Pipeline Design for the Danish North Sea", 6th International Conference on the Internal and Ex-ternal Protection of Pipes, Nice,

France 5-7 November 1985, pp. 189-202.

Nielsen, N.J.R.; Pedersen, P.

Tern-drup; Grundy, A.R. & Lyngberg B.: "New Design Criteria for Upheaval Creep of Buried Subsea Pipelines", Proc. of the Seventh Inter. Conf. on Offshore

Mechanics and Artic Eng., OMAE, Hous-ton, vol.

v,

pp. 243-250, 1988. Pedersen, P. Terndrup & Jensen, J.

Juncher: "Upheaval Creep of Buried Heated Pipeline with Initial Imper-fections", J. of Marine Structures, Vol. 1 pp. 11-22, 1988.

Pedersen, P. Terndrup & Michelsen, J.: "Large Deflection Upheaval

Buck-ling of Marine Pipelines", Proc.

Behaviour of Offshore Structures

(BOSS), Trondheim, Norway, Vol. 3, pp.

965-980 June 1988.

Mousselli, A.M.: "Pipe Stresses at the Seabed during Installation and Trenching Operations", Proc. Offshore Technology Conference, Paper no. OTC

2965, 1977. f3]

(8)

(a)

(b)

2" PUP Epoxy Coating

Fig. 1 Pipeline Build-up for the 8./3. Rolf to Gorm

Piggy Back Line.

2 meter 3

Epoxy Coating 3" GAS Lift Line

2" Concrete Coating PE Sleeve

8" OIL! GAS Line

588

Geometry of the Exposed Pipe Section at KP 0.3. As-found Configuration.

Configuration after Complete Cool Down.

FloId Joint 025

rorn InfIll

455 530

309 400

Fig. 3 Retrieved Pipe Section Fig. 4 r Severe Foam Shrinkage in

from KP 0.3. Line Pipe from KP 0.3.

1

0

Fig.

(a)

(9)

.5

.4

LI

Line of symmetry

Moment distribution

Fig. 5

:

Equilibrium Form and Moment Distribution

for a Partly Untrenched Pipeline.

Max. Moment normalized by ELI Lc

""\\

H/Lc ..I0

NU= .08

.06

Non-dimensional Bending Moment

as a Function of Half the

Untrenched Length.

589 :6 :8 .9 LO Li! Lc

Fig. 6:

.3- .2 -.2 .3 .4 .7

(10)

350 A T I 300 250 200 15 +100 .Gottm 50

Trench bottom

0.5m imperfection Amplitude 0 Or

v---

10 20 30 40 50 meter Symbols

:

As-built Survey Measurements

lune 1985

FOOLF

.3

0: SBP Survey Measurements September *88

0.5

A

P0

,k40

D = 0.219'm

t 0.014 m

IniViol Impert Length 5010

Pipe Total Length .200

Rigid Flat Foundation

46 m

25 50 75, 100 125 150 175

Uplifted Length. tit

Fig, a : Example of "Classical Upheaval Response Calculations.

590

Sea bed

Curve fitted

As-built "Prop imperfection

through 1986 SBP Survey

1m

Fig_ 1 Observed Upheaval Creep, of an Initially 'Imperfect" Pipe Section-1

Fig. 9 Pipe Configuration at the

of the Trench., 11

2:rn

LU q.

'Edge !I

(11)

100-0 A.0.02 m Sea Floor _ No A.2cm 6f -0-'

.../

....

../

.../.t<C(3'''k"

.""'

./..-. .. ...°- ...-. ..---

---

--- 40,

---

.---.

_----"bk''

---

--

.----

---_---

--

--

---

--...---

0--

--

....--

_

----

---

.,--

---

--I 1

2L0 = 24.5m

No

e-°

50-Heavy, linear beam on flat foundation.-'

Non-I ineor method. elasto-plastic pipe (X52)

Upheaved Pipeline Sea Floor

Uplift A (m)

Fig. 11 : Post-buckling Equilibrium Curves

for the 8" Rolf Pipeline.

591

115 2.0

04 0.6 0.8 1.0 1.2 1.4 1.6 1.8 2D

Minimum trench depth H cm)

Fig. 10 : Critical Temperature to prevent

Upheaval Creep of an "Imperfect", Buried Pipe Section.

0 10 Lift-off oint X

T.

(C)

100 50 200

AT°

(C°)

150-6I-0.2m I

(12)

60 50- 40- 30- 20- 10-0 o

Temperature at "IMPERFECT LOCATION"

II

Sea bed 11.7m i05m 46m 0:1 0.2 0;3 0:4 05 0.6 0.7 08 UPLIFT DISPLACEMENT (m)

Fig. 12 : Influence of Geometric Pipe

Imperfection on Upheaval Behaviour.

592

80

AT Pipe with NO GEOMETRIC IMPERFECTION

70- "STRESS FREE" PIPE

(°C)

Cytaty

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